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Q1 33027

 

24th July 1951

Locomotive Casualty Report (Mechanical)

No.33027 (Q1) Clack Valve Failure

 

On Tuesday 24th July 1951 Q1 locomotive no.33027 was working the 1.15am freight from Snodland to Maidstone when its no.1 Injector clack valve seized at Snodland causing a sixty minute delay to the train. The valve was reseated and cleaned with the locomotive return to traffic.

Gillingham Driver Mick Bruce retained copies of the Locomotive Casualty Report (Mechanical), Guard’s Report to Driver or Motorman and Engineman’s Report passing them onto the son of George Blakeman (the train’s fireman).

 

A close-up of a paper

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Locomotive Casualty Report (Mechanical) - front

© Motorman Blakeman

 

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Locomotive Casualty Report (Mechanical) - rear

© Motorman Blakeman

 

On 27th July 1951, Gillingham’s Loco Shed Master [E. Smith] recorded on the rear page of the Locomotive Casualty Report (Mechanical) that the no.1 Injector clack valve had previously been reported on 18th July 1951 as

No.1 Clack keeps sticking up. Valve cleaned and reseated”.

On 6th August 1951 Stewart’s Lane signed on behalf of G.L. Nicholson (Divisional Motive Power Superintendent) that

The clack was fast owing to being filled up with water sediment apparently trouble is experienced at Gillingham from this cause to blame on staff”.

 

 

 

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Guard’s Report to Driver or Motorman
(Stock 1152C 7/47)

© Motorman Blakeman

 

Maidstone Guard’s (H. Stroud) Report to Driver identified 60 minutes lost with the driver stating

No.1 injector boiler clack stuck up. No.2 injector only working partially not sufficient to maintain boiler, necessary to get clack down which I managed to do after procuring a ladder to get to clack based. This accrued on standing time of train”.

Gillingham Driver (E. Snipp) signed off on the form.

Gillingham Depot Supervisor (E. Smith) remarked

Please connect with driver’s report sent 26th inst”.

 

 

 

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Engineman’s Report – Stamped 26th July 1951
(Stock 858 5/49)

© Motorman Blakeman

 

In his Engineman’s Report of the 1.15am Snodland to Maidstone train on Tuesday 24th July 1951 Gillingham Driver E. Snipp made on Tuesday 24th July 1951 to Gillingham Shed Master E. Smith stated

Sir, immediately on starting time of above train the boiler clack of No.1 injector was only partially working and was not sufficient to maintain the boiler. I procured a ladder to reach clack base and eventually managed to get the clack down. I was ready to start train at 2.0am. Time of occurrence 1.10am started train 2.15am. Load of train 50 vehicles = 65”.

 

 

Locomotive Fireman

Fireman George Blakeman joined British Railways in 1949 as a cleaner before becoming a fireman based at Gillingham in 1950. With the forthcoming Kent Coast electrification he left the railway in 1954 in favour of the boiler house at Bart’s Hospital, Chatham. His son joined British Rail in 1978 at Stonebridge Park, moving to Gillingham in 1982 and retiring as a motorman in 2022.

© Motorman Blakeman

 

 

 

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